AAIB investigation to MCR-01 Club, G-DGHI
Runway excursion after landing, Fridd Farm, Kent, 20 September 2015.
Summary:
皇冠体育app pilot was conducting a local flight from a farm strip where the aircraft was based. On his return, about 2 nm away from the strip, the engine misfired. 皇冠体育app pilot then flew past the strip to assess the wind indicated by the strip鈥檚 windsocks. As he did so the engine misfired again. 皇冠体育app wind was light and variable and he positioned the aircraft for a landing on Runway 14.
皇冠体育app pilot established the aircraft slightly high and slow on the final approach because of large oak trees in the runway undershoot, so that if the engine failed before crossing them he would be able to land beyond them.
皇冠体育app pilot then judged that the aircraft was too high on the approach and initiated a go-around on short final. Soon after achieving full power the engine misfired again and then stopped. 皇冠体育app pilot attempted to avoid an area of soft ground. 皇冠体育app aircraft landed in the overshoot of the strip on an area of grass before coming to rest in an adjacent field of crops where the nose wheel dug in and the aircraft came to a stop.
皇冠体育app pilot vacated the aircraft uninjured. 皇冠体育app aircraft sustained damaged to its propeller, nose wheel and cowls.
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