Airbus A321-231, G-MEDJ, 24 August 2010

Airbus A321-231, G-MEDJ

Summary:

皇冠体育app aircraft suffered an electrical malfunction during a scheduled night flight between Khartoum (Sudan) and Beirut (Lebanon). 皇冠体育app more significant symptoms included the intermittent failure of the captain and co-pilot鈥檚 electronic displays and the uncommanded application of left rudder trim, which was not annunciated to the flight crew. 皇冠体育app flight crew also reported that the aircraft did not seem to respond as expected to control inputs. A large number of ECAM messages and cautions were presented on the pilots鈥� electronic display units. 皇冠体育app uncommanded rudder trim caused the aircraft to adopt a left-wing-low attitude and deviate to the left of the planned track. Normal functions were restored after the flight crew selected the No 1 generator to OFF in response to an 鈥�ELEC GEN 1 FAULT鈥� message. 皇冠体育app aircraft landed safely at Beirut.

皇冠体育app No 1 generator was replaced, after which the fault did not recur. Damage was found on an electrical lead on the No 1 generator, but it could not be determined whether this had caused the symptoms experienced during the incident.

皇冠体育app aircraft manufacturer notified operators of this incident by issuing OIT 999.0105/10 on 19 November 2010 and also updated the Quick Reference Handbook procedure for 鈥�Display Unit Failure鈥� to include a check of the rudder trim position.

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Published 10 December 2014